Resolution of solder voids in pin-in-hole product
ing improvements were implemented. A fil- ferent hypotheses through experiments and and Gary Gao.
tration system was installed in the recircu- determine the ultimate cause of the solder
lation path of the permanganate desmear- voids. The solder voids which formed references
ing bath to remove residue and lower the were as a result of the residue that was left 1. Acceptability of Electronic Assemblies,
chance of debris attaching onto hole walls. in the PTHs during the sweller/desmear IPC-A-610D, IPC Bannockburn, IL.
To further drive down the dppm rate, addi- operation. This residue was plated into 2005. pp. 5-10, 7-50 to 7-52.
tional actions were taken to minimize the copper nodules. When these copper nod- 2. Kang-Wook Lee, “Mechanism of E&E
chance of copper nodule formation and ules went through the wave solder process, PCB Void Formation (version 1)”
micro copper void formation. The water the thermal energy in the wave volatilized 3. Safdar Ishtiaq, and Ahmed Faisal,
rinse pressure in the deburr line was in- the residual sweller solvent ‘popcorning’ “The implementation of via-in-pad
creased in order to enhance the efficiency the nodule, releasing the gas to form solder interconnects to increase PBC circuit
with which drill debris is flushed away voids in the PTHs. Filtration was imple- density: filled via-in-pad processes are a
from PTHs therefore preventing it from mented to remove the residue by-product way to achieve an intermediate density
contaminating the desmear bath. Periodic from the process. It was then demonstrated increase for a minimal additional cost.”
cleaning of the permanganate desmear that this did nearly eliminate the solder Printed Circuit Design & Manufac-
bath was implemented to avoid excessive void defect. ture, Oct 2007.
residue accumulation. 4. Clyde F. Coombs, Jr., “Printed circuits
acknowledgements handbook”, McGraw-Hill, New York,
summary We the authors wish to thank our families 1995, p28-30.
Once the problem was identified, a cross- who were very understanding while we 5. R. J. Klein Wassink, Soldering in Elec-
company team was established to identify were working on this problem. We further tronics. Electrochemical Publications
the root cause of the solder void phenom- wish to thank our co-workers who were Limited, Scotland, 1984. pp. 271-272,
ena. The team was able to examine the much help; the CMs who worked with us, 310-311.
evidence through failure analysis, test dif- the IBM Fishkill Materials Analysis team
Europe
USA/Canada
¤Z
½ès
UK/Ireland
Mexico
India
한국
Brasil
Íß´
Magyarország
globalsmt.net.cn
brasil.globalsmt.net
globalsmtindia.in
hungary.globalsmt.net
japan.globalsmt.net
korea.globalsmt.net
mexico.globalsmt.net
uk.globalsmt.net
Opening up a world of
www.globalsmt.net
opportunities
www.globalsmt.net Global SMT & Packaging – February 2009 – 27
Page 1 |
Page 2 |
Page 3 |
Page 4 |
Page 5 |
Page 6 |
Page 7 |
Page 8 |
Page 9 |
Page 10 |
Page 11 |
Page 12 |
Page 13 |
Page 14 |
Page 15 |
Page 16 |
Page 17 |
Page 18 |
Page 19 |
Page 20 |
Page 21 |
Page 22 |
Page 23 |
Page 24 |
Page 25 |
Page 26 |
Page 27 |
Page 28 |
Page 29 |
Page 30 |
Page 31 |
Page 32 |
Page 33 |
Page 34 |
Page 35 |
Page 36 |
Page 37 |
Page 38 |
Page 39 |
Page 40 |
Page 41 |
Page 42 |
Page 43 |
Page 44 |
Page 45 |
Page 46 |
Page 47 |
Page 48 |
Page 49 |
Page 50 |
Page 51 |
Page 52 |
Page 53 |
Page 54 |
Page 55 |
Page 56