This page contains a Flash digital edition of a book.
Here, the design changes at the top of the casting are shown with the red model representing the original drawing and the white model being the new design. The arrows indicate areas of the cross-section where changes were made.


“We originally had a drain hole in the


rear,” Sigelakis said. “We eliminated the drain hole and instead created two chan- nels under the tongue [to allow drainage]. Additionally, it protects the tongue and helps hold the core in place.” Applegate said several other chang- es completed the reduction in the num-


ber of cores used, including a change in the draft on the front cap at the top of the hydrant so that the cores could be drawn naturally (i.e., removed from the sand mold without damaging it). On the interior of the casting, the engi- neering team cored the hole where the ball screw would go to reduce porosity.


Finally, mass was removed from the inside channels so those cores could be drawn naturally, as well. “The cost of the tooling was much less after the redesign,” Sigelakis said. “Much, much less.” The new core design also eliminated a significant number of man-hours at


JULY/AUGUST 2011


METAL CASTING DESIGN AND PURCHASING


43


Page 1  |  Page 2  |  Page 3  |  Page 4  |  Page 5  |  Page 6  |  Page 7  |  Page 8  |  Page 9  |  Page 10  |  Page 11  |  Page 12  |  Page 13  |  Page 14  |  Page 15  |  Page 16  |  Page 17  |  Page 18  |  Page 19  |  Page 20  |  Page 21  |  Page 22  |  Page 23  |  Page 24  |  Page 25  |  Page 26  |  Page 27  |  Page 28  |  Page 29  |  Page 30  |  Page 31  |  Page 32  |  Page 33  |  Page 34  |  Page 35  |  Page 36  |  Page 37  |  Page 38  |  Page 39  |  Page 40  |  Page 41  |  Page 42  |  Page 43  |  Page 44  |  Page 45  |  Page 46  |  Page 47  |  Page 48  |  Page 49  |  Page 50  |  Page 51  |  Page 52  |  Page 53  |  Page 54  |  Page 55  |  Page 56  |  Page 57  |  Page 58  |  Page 59  |  Page 60